Not a restoration.
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- 937carrera
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Re: Not a restoration.
Let's hope postie turns up tomorrow for you.
Bleed ring looks good, when are you going into production ?
Bleed ring looks good, when are you going into production ?
1981 RHD 2.0 Aircooled Leisuredrive project, CU engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
- itchyfeet
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Re: Not a restoration.
nice ring, you will be making the large water pipe next.
- bigbadbob76
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Re: Not a restoration.
937carrera wrote:when are you going into production ?
When I have time on my hands. yeah, that'll be never then.
itchyfeet wrote:you will be making the large water pipe next.
Believe me, if I could bend and weld stainless I would.
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- bigbadbob76
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Re: Not a restoration.
Cheers 300CE, the wife thinks it looks very steampunk and we should do all the pipes in copper.
That'll be the royal WE then.
That'll be the royal WE then.
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- bigbadbob76
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Not a restoration.
Water pipe arrived so o fitted that and filled up with G13, Then i primed the oil pump, threw some fuel down the carb, turned on the ignition, went round the back, connected a wire to my hot start relay so i could start it from the engine bay and............
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- 937carrera
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Re: Not a restoration.
She fired up and ran well after a few initial coughs
1981 RHD 2.0 Aircooled Leisuredrive project, CU engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
- bigbadbob76
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Re: Not a restoration.
[FACE WITH TEARS OF JOY][FACE WITH TEARS OF JOY] it coughed a bit but didn't start. I checked it was pumping fuel, yep, I got the timing light out and checked timing. It was well off so a quick tweak sorted that and..... tapatalk won't let me post video. Grrrr...
Anyway.... it runs well. Doesn't clatter much, doesn't smoke much, no flames. A few minor coolant leaks from hoses that needed nipped up, including one from the stainless pipe behind the pulleys where it's hard to get at. no oil leaks, but in spite of tying up the clutch lever, the clutch has jammed. Bugger, think i'll pull the g.box off to sort the release bearing.
Anyway.... it runs well. Doesn't clatter much, doesn't smoke much, no flames. A few minor coolant leaks from hoses that needed nipped up, including one from the stainless pipe behind the pulleys where it's hard to get at. no oil leaks, but in spite of tying up the clutch lever, the clutch has jammed. Bugger, think i'll pull the g.box off to sort the release bearing.
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- bigbadbob76
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Re: Not a restoration.
Had to upload to Flikr.
lets see if this works....
https://www.flickr.com/photos/mm0rbz/42 ... datetaken/
lets see if this works....
https://www.flickr.com/photos/mm0rbz/42 ... datetaken/
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- 937carrera
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Re: Not a restoration.
Nearly right on my guess, you should be very pleased
I think you have to be very careful when putting the release bearing on. When I changed my guide sleeve I did it 2 or 3 times before being happy that the side clips were in the right place. And then there was the fun of getting the rod for the slave cylinder in the right place.
A few little bits and pieces to do, you should be going out for a drive this weekend
ps...... you tease
1981 RHD 2.0 Aircooled Leisuredrive project, CU engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
-
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Re: Not a restoration.
Have you ever seen an unhappy fool?
88 Transporter with hitop camper conversion, 1.6td.
88 Transporter with hitop camper conversion, 1.6td.
- 937carrera
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Re: Not a restoration.
bigbadbob76 wrote:Had to upload to Flikr.
lets see if this works....
https://www.flickr.com/photos/mm0rbz/42 ... datetaken/
Video worked fine, nearly 2.5 bar at cold idle
1981 RHD 2.0 Aircooled Leisuredrive project, CU engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
- bigbadbob76
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Re: Not a restoration.
cheers, here's another-
https://www.flickr.com/photos/mm0rbz/42 ... datetaken/
The knocking noise is the silencer hitting the chassis, that's sorted now.
Oil is just cheap flushing oil so pressure should be better once I get some decent oil in there.
I havn't got it hot enough to open the thermostat yet so the coolant isn't bleeding but I'm getting there.
Glad to hear it run.
https://www.flickr.com/photos/mm0rbz/42 ... datetaken/
The knocking noise is the silencer hitting the chassis, that's sorted now.
Oil is just cheap flushing oil so pressure should be better once I get some decent oil in there.
I havn't got it hot enough to open the thermostat yet so the coolant isn't bleeding but I'm getting there.
Glad to hear it run.
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.
- 937carrera
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- Posts: 3599
- Joined: 05 Apr 2015, 19:29
- 80-90 Mem No: 16333
- Location: N Yorks.
Re: Not a restoration.
4 bar at cold idle and no smoke / leaky bits, sounds sweet
1981 RHD 2.0 Aircooled Leisuredrive project, CU engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
1990 RHD 1.9 Auto Sleeper with DF/DG engine
- bigbadbob76
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- Posts: 1733
- Joined: 07 Nov 2016, 14:41
- 80-90 Mem No: 15707
- Location: Isle of Skye
Re: Not a restoration.
yep, 4 bar with the choke on/fast idle. And dropped to 2.5 as it warmed up and the choke came off and the idle speed dropped.
no water in the oil (yet).
Tappety rattle that should go away after a run.
Clutch is pissing me off as I thought I'd taken steps to stop it happening.
no water in the oil (yet).
Tappety rattle that should go away after a run.
Clutch is pissing me off as I thought I'd taken steps to stop it happening.
'86 1.9 DG, 4 spd, tintop, camper conversion.
Split case club member.
Split case club member.